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HomeMy WebLinkAboutSB989 2023 Appendix VII Underground Storage Tank Secondary Containment Testing Report Form CERS = California Environmental Reporting System, ICC = International Code Council, ID = Identification, NA = Not Applicable, UDC = Under-Dispenser Containment, Page 1 of 5 TYPE OF ACTION ☐ Installation ☐ Repair ☐ 6 Month X 36 Month CERS ID 1002403 Test Date 10/31/2023 Facility Name Chevron Facility Address 1125 Coffee Rd City Bakersfield ZIP Code 93308 Company Performing the Test Advanced Compliance Phone 6617064321 Mailing Address 4007 Brae Burn Dr Bakersfield Ca 93306 Service Technician Performing Test Bradley Hinsley Contractor/Tank Tester License Number 971259 ICC Number 8835007 ICC Expiration Date 8/8/2025 Manufacturer and Test Equipment Training Certifications Expiration Date ICC Service Techican 8/8/2025 INCON STS 10/20/2023 Test Procedures Used Components Tested PEI/RP1200-19 Sect. 4. Tank Annular PEI/RP1200-19 Sect. 5. Line Secondary PEI/RP1200-19 Sect. 6. Containment Sump I hereby certify that the secondary containment was tested in accordance with California Code of Regulations, title 23, division 3, chapter 16, section 2637; that required supporting documentation is attached; and all information contained herein is accurate. I understand that test procedures shall be made available upon request by the governing authority. Service Technician Signature Date 10/31/2023 Total # of Pages 1. FACILITY INFORMATION 2. SERVICE TECHNICIAN INFORMATION 3. TRAINING AND CERTIFICATIONS 4. TEST PROCEDURE INFORMATION 5. CERTIFICATION BY SERVICE TECHNICIAN CONDUCTING TEST Underground Storage Tank Secondary Containment Testing Report Form All tests marked “Fail” and any repairs made before or during the tightness test must be described in the COMMENTS section. Page 2 of 5 Test Method Developed by ☐ Manufacturer ☐ Industry Standard X Professional Engineer Test Type ☐ Pressure X Vacuum ☐ Hydrostatic Test Equipment Used: Annular Testing Setups Tank ID 87 91 Diesel Tank Manufacturer Unknown Unknown Unknown Tank Capacity 12,022 12,022 12,022 Test Start Time 08:20 08:35 10:30 Initial Reading -10.0 InHg -10.0 InHg -10.0 InHg Test End Time 09:20 09:35 11:30 Final Reading 0.0 InHg 0.0 InHg 0.0 InHg Change in Reading 10.0 InHg 10.0 InHg 10.0 InHg Pass/Fail Criteria +/- 0.0 InHg +/- 0.0 InHg +/- 0.0 InHg Tightness Test Results ☐ Pass X Fail ☐ Pass X Fail ☐ Pass X Fail ☐ Pass ☐ Fail Test Method Developed by ☐ Manufacturer ☐ Industry Standard X Professional Engineer Test Type X Pressure ☐ Vacuum ☐ Hydrostatic Test Equipment Used: Line Secondary Testing Setups Pipe Run ID 87 91 Diesel Pipe Manufacturer Unknown Unknown Unknown Test Start Time 08:10 08:15 08:20 Initial Reading 5.0 PSI 5.0 PSI 5.0 PSI Test End Time 09:10 09:15 09:20 Final Reading 2.0 PSI 5.0 PSI 1.0 PSI Change in Reading 3.0 PSI 0.0 PSI 4.0 PSI Pass/Fail Criteria +/- 0.0 PSI +/- 0.0 PSI +/- 0.0 PSI Tightness Test Results ☐ Pass X Fail X Pass ☐ Fail ☐ Pass X Fail ☐ Pass ☐ Fail Pipe Run ID Pipe Manufacturer Test Start Time Initial Reading Test End Time Final Reading Change in Reading Pass/Fail Criteria Tightness Test Results ☐ Pass ☐ Fail ☐ Pass ☐ Fail ☐ Pass ☐ Fail ☐ Pass ☐ Fail Additional copies of this page may be attached. 6. TANK SECONDARY CONTAINMENT TEST 7. PIPE SECONDARY CONTAINMENT TEST Underground Storage Tank Secondary Containment Testing Report Form All tests marked “Fail” and any repairs made before or during the tightness test must be described in the COMMENTS section. Page 3 of 5 Test Method Developed by ☐ Manufacturer ☐ Industry Standard X Professional Engineer Test Type ☐ Pressure ☐ Vacuum X Hydrostatic Test Equipment Used: Incon STS Sump/UDC ID 87 STP 91 STP Diesel STP UDC 1/2 Sump Manufacturer Unknown Unknown Unknown Unknown Sump Depth (inches) 63 In 63 In 63 In 44 In Sump Bottom to Top of Highest Pipe Penetration (inches) 35 In 34 In 34 In 27 In Test Start Time 12:44 1:14 12:02 12:03 Initial Reading 4.7593 4.4474 5.7532 3.4374 Test End Time 12:59 1:29 12:17 12:19 Final Reading 4.7052 4.4472 5.7508 3.4361 Change in Reading 0.0541 0.0002 0.0024 0.00013 Pass/Fail Criteria +/- 0.0020 +/- 0.0020 +/- 0.0020 +/- 0.0020 Tightness Test Results ☐ Pass X Fail X Pass ☐ Fail ☐ Pass X Fail X Pass ☐ Fail Sump/UDC ID UDC 3/4 UDC 5/6 UDC 7/8 UDC 9/10 Sump Manufacturer Unknown Unknown Unknown Unknown Sump Depth (inches) 44 In 44 In 44 In 44 In Sump Bottom to Top of Highest Pipe Penetration (inches) 27 In 27 In 27 In 27 In Test Start Time 12:03 11:43 11:43 1:39 Initial Reading 7.1031 3.7556 5.1341 5.7480 Test End Time 12:19 11:58 11:58 1:54 Final Reading 6.6147 3.7554 4.6665 5.4470 Change in Reading 0.4884 0.0002 0.4676 0.3010 Pass/Fail Criteria +/- 0.0020 +/- 0.0020 +/- 0.0020 +/- 0.0020 Tightness Test Results ☐ Pass X Fail X Pass ☐ Fail ☐ Pass X Fail ☐ Pass X Fail Additional copies of this page may be attached. 8. SUMP/UDC TEST Underground Storage Tank Secondary Containment Testing Report Form All tests marked “Fail” and any repairs made before or during the tightness test must be described in the COMMENTS section. Page 4 of 5 Test Method Developed by ☐ Manufacturer ☐ Industry Standard X Professional Engineer Test Type ☐ Pressure ☐ Vacuum X Hydrostatic Test Equipment Used: Sump/UDC ID UDC 11/12 Sump Manufacturer Unknown Sump Depth (inches) 44 In Sump Bottom to Top of Highest Pipe Penetration (inches) 27 In Test Start Time 1:39 Initial Reading 5.9932 Test End Time 1:54 Final Reading 5.7032 Change in Reading 0.2900 Pass/Fail Criteria +/- 0.0020 Tightness Test Results ☐ Pass X Fail ☐ Pass ☐ Fail ☐ Pass ☐ Fail ☐ Pass ☐ Fail Sump/UDC ID Sump Manufacturer Sump Depth (inches) Sump Bottom to Top of Highest Pipe Penetration (inches) Test Start Time Initial Reading Test End Time Final Reading Change in Reading Pass/Fail Criteria Tightness Test Results ☐ Pass ☐ Fail ☐ Pass ☐ Fail ☐ Pass ☒ Fail ☐ Pass ☐ Fail Additional copies of this page may be attached. 8. SUMP/UDC TEST (continued) Underground Storage Tank Secondary Containment Testing Report Form All tests marked “Fail” and any repairs made before or during the tightness test must be described in the COMMENTS section. Page 5 of 5 87 & Diesel lines failed due to torn boots in Disp 1/2(DSL) and 9/10(87). Annulars failed, suspect heat causing failures. 87 & Diesel STP Sumps, UDC 3/4, 7/8, 9/10 and 11/12 failed. All failures must be repaired and retested. All else passed. 9. COMMENTS